The first frost came and my gardening days are pretty much done, we are adjusting to the addition of our youngest son, and the patio is finally complete (mostly). I now have a few moments here and there to escape to the garage and play. I decided no to mock up the radiator in the donor front clip due to space constraints. Instead, I started to cut it down to usable panels. I can walk all the way around the bug without running into stuff for the first time in a long time.
Thursday, October 15, 2009
Wednesday, July 8, 2009
For anyone interested...sorry for the delay.
This project has been put on hold for the following reasons:
The patio also includes a concrete pad outside of the garage which should help in moving this project along faster.
- garden prep and planting
- patio prep and installation
- new addition to the family
The patio also includes a concrete pad outside of the garage which should help in moving this project along faster.
Monday, February 23, 2009
Here's the idea...
I unfortunately found some more metal that will need to be replaced on the donor front clip. More practice...
Thursday, February 19, 2009
Removing spot welds

I also experimented with removing the decklid seal retaining strips. I found the easiest way to do this is to cut or grind the first two or three welds then pull the strip away while wiggling it back and forth(2/23/09--this method didn't seem to work for the remaining strips unless I ground down the spot welded area a bit first). The welds break right off without distorting the base metal. When the strip is removed all that is left is a small piece of metal to grind down at each weld--less than is left when using a spot weld cutter.
Sunday, February 15, 2009
Beetles = Rust
Yesterday I put my skills to work repairing a rust hole in the panel that I am going to graft onto my bug. Up to this point all of my welding has consisted of stick or MIG on relatively thick steel. So this is my first attempt at sheet metal work. Fortunately I had a very inconspicuous place to start.
The bumper bracket area on the donor piece had rusted through, so I began the repair by cutting a good piece of steel out from the same donor piece that I will not need. I cut it to fit the place that was rusted out. I then traced the piece out on the rusted area. Once the rusted area was removed I fine tuned the fit and tacked it into place. I then continued adding more tack welds--cooling in between--until the seam was complete. A few passes with a flap disc and things looked pretty good for a rookie.
Things that went well:
I used the suggested settings on my welder and didn't have to adjust the feed or amperage.
Good weld penetration.
Only a couple of burn throughs that I was able to fix by holding a piece of brass behind the hole while filling it in.
Minimal warpage.
Things I would have done differently:
I wouldn't have made the fit so tight--one part of the patch ended up overlapping after applying a few tack welds which was difficult to fix.
I would have cleaned the weld area better--one area that was tough to get to had a little surface rust causing a few messy welds.
Other notes:
I found that my welder could easily handle a gap of up to about 1/16".
Clean metal is necessary for a clean weld.
I found that I was able to create a smoother arc when I clipped the wire before each weld and when I cleaned up previous welds that I was welding over with a wire brush.
The new piece with a few tacks (and one burn through)
The finished product
The back side--to show weld penetration
This gift from Emily made this job a
The bumper bracket area on the donor piece had rusted through, so I began the repair by cutting a good piece of steel out from the same donor piece that I will not need. I cut it to fit the place that was rusted out. I then traced the piece out on the rusted area. Once the rusted area was removed I fine tuned the fit and tacked it into place. I then continued adding more tack welds--cooling in between--until the seam was complete. A few passes with a flap disc and things looked pretty good for a rookie.
Things that went well:
I used the suggested settings on my welder and didn't have to adjust the feed or amperage.
Good weld penetration.
Only a couple of burn throughs that I was able to fix by holding a piece of brass behind the hole while filling it in.
Minimal warpage.
Things I would have done differently:
I wouldn't have made the fit so tight--one part of the patch ended up overlapping after applying a few tack welds which was difficult to fix.
I would have cleaned the weld area better--one area that was tough to get to had a little surface rust causing a few messy welds.
Other notes:
I found that my welder could easily handle a gap of up to about 1/16".
Clean metal is necessary for a clean weld.
I found that I was able to create a smoother arc when I clipped the wire before each weld and when I cleaned up previous welds that I was welding over with a wire brush.
Here is the piece that was removed
heck of a lot easier than with my old helmet
Tuesday, January 27, 2009
Summer...so far away...
Monday, November 24, 2008
This front clip also came with the fenders, lights partial wiring harness, spedo, dash, original Blaupunkt radio, wiper motor, etc... I don't know if any of it works. I don't need any of it for this project so I will probably sell it online for cheap.
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